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magnet former and coils are gradually increasing. If the heat load to the magnet
does not result in any part of the coils rising above the critical temperature (9.7
K) to go resistive then a quench will not occur. Once the beam is well positioned
on target location it is necessary to study what the maximum intensity is that can
be achieved without the target magnet quenching. The UVA simulations indicate
that running at 1×1012 proton per second for 4.4 seconds should be possible but
this pushes the limit.

Once the magnet quenches, we will need a Hall access to fill the magnet and
setup for the next run.  After each quench about 100 LHe is required to refill.
The system can be used again once the magnet space is refiled and the magnet is
fully cooled again, this takes about 1-4 hours including fill time. Once the system
is ready and ramped up again a beam intensity just below the last beam intensity
should be used to pin-point the quench threshold.  Because of the LHe and recovery
time this part of commissioning should be expected to take two or three weeks.

We will likely need more than 10 quenches for this phase of commissioning:


2 for when we first put the beam on target (leeway): These are accidental and shouldn't
happen unless we mess up with beam width or beam/target position which should all be
confirmed before we ramp up the target magnet. Starting at 5×1010 we should increase in
steps of 5×1010 until we get a quench running for10 for 10 spills before increasing for each step.

3 for when we get the limit and reproduce it for a full target cell of NH3.
3 for when we get the limit and reproduce it for a full target cell of ND3.
2 for when we are checking this limit for each target cell position.

Based on what the numbers are we may try to reconfigure the target cell to hold less material,
or rebuild the ladder to have less aluminum, or modify the NMR coils, or other such changes,
and then try again.  We will also have the option of running the magnet pump at a higher rate
to increase the cooling power in the magnet reservoir while decreasing the temperature of the coils.
The KNF magnet pump can run over 100 SLPM so its possible to cool the magnet below 2.5 K
with forced convention to reduce the heat load to the coils during a spill.  This of course increases
helium consumption.